http://dailyhurricane.com/2010/08/adm-allen-confused---so-now-is-everybody-else.htmlAdm. Allen Confused - So, Now, Everybody Else is, Too
By eljefebob on August 12, 2010 10:00 AM
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All was right with the world. Except, it wasn't. Day before yesterday, Adm. Allen announced they were going to start a "pressure test", babbling about the annulus and raising the ominous spectre that they are still actually communicated to the reservoir. Wells confirmed that fear in the afternoon, admitting that they indeed had 4,200 psi on the well when it's supposed to be dead. At the seafloor, the well should have no more than 2,200 psi on it, and conceivable less, if the hydrostatic of the mud in the closed well had overcome reservoir pressure. Then it got really confusing. Wells said that it wouldn't hold 4,200 psi because of "bubbles" leaking out of the wellhead, implying that they are pumping on it to keep it there, but that they're going to "test" it by relieving pressure. ?? Also, the more Adm. Allen explains what's going on, the more the press gets confused. Hell, I understand this business and I'm confused.
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In actuality, this "static kill" did nothing that BP and Allen said it would do. Certainly the well is not dead or "static". It hasn't accelerated the relief well, but it has obscured the well's pressures, making it more difficult to kill. Hence, these new tests to figure out what's going on. BP and the government don't really have a clue where the 2,300 barrels of mud and 500 barrels of cement went. They originally claimed it all went down the casing and out to the reservoir. I would set the probability of that actually having happened at zero. Here's why: The positive test on the casing the night of the blowout was rock solid. The casing was good. It is possible that they may have collapsed the production casing during the blowout, but that would have been relatively high up in the wellbore, probably where they had displaced with seawater on the inside. If that happened, it would be communicated with the backside. In addition, at the bottom of the production casing is a float shoe, 134 feet of cement in the shoe track, then a float collar, then 2 cementing plugs with probably cement on top of those. Oh, and don't forget about the 3,000 feet of drill pipe hanging inside all of that. There is no way, unless that entire float assembly blew off, that they pumped down the casing and up the backside. On top of all that, there are HUGE lost circulation zones both below and above the reservoir. During drilling they lost 3,000 barrels of mud trying to drill that last section.
So, where did all the mud and cement go? It likely went down the backside of the production casing and either out through some damage that was caused during the aborted top kill, or out the lost circulation zone right below the 9 7/8" liner at 17,100. The fact that they're getting pressure now tells me that they are indeed communicated to the reservoir below, probably obscured by the fact that they now have mud strung through the annulus. If they are indeed communicated, pressure will build on the wellhead, which is exactly what's happening. Adm. Allen pledged to get BP to release the pressure data 3 days ago. The next day, when asked about it, he said it was released, but "nobody can find it." The data is still AWOL.
So, now, here we sit, waiting on weather again, and then we're going to pressure test a well that's supposed to be dead instead of getting the relief well finished. The press is confused; the public is bored.